Struggling with a smoky and burbly 2e2
Posted: Sun Nov 10, 2024 12:10 pm
I have a Mk2 '88 Scala with EX engine and Pierburg 2e2.
Timeline:
Fuel seemed to be getting up to the carb fine - there was the tiniest little air bubble in the top corner of the inline filter, and I had also replaced all the fuel lines and jubilee clips.
On the ignition side of it, I had before getting the car on the road replaced essentially the entire ignition system: spark plugs, ht leads, tci, dizzy rotor, coil.
This led me to believe that the problem lay somewhere with the carb, thinking it might be a gunked up jet or drilling or something similar, so I ordered some bits up and did the following:
After a lot of trial and error I found that screwing the mixture screw (the one accessible via the bung on the airbox) fully in, then unscrewing it by two full turns seemed to allow the engine to start without the carb popping and spewing a ton of smoke.
This is what happens when starting it up:
I subsequently came back after a few hours to let it sit and go back to "cold"/ambient temps for the purpose of repeatability and tried the same but turning the screw counter clockwise. Effectively the same thing happened.
I also ran the engine up once, messing with nothing, just letting it get hot, and it seemed happy to throttle up, but was stilling spewing smoke everywhere.
While running the fuel filter was chock full of fuel, and after it cut out there was still plenty of fuel in the filter. The mechanical fuel pump and air/vapour seperator/pressure regulator have both been replaced. It used to struggle to start and I had to pump the throttle once or twice depending on how long I had left it without starting it for the couple of months when I got it ready to go back on the road, after replacing the air/vapour seperator it would start happily when turning the key, now I have to give it a pump to get it run, but it may just be that method of bleeding the air doesn't get all the air out (I split the return line, blow air into return to the tank, let the fuel filter all fill up and make sure the flow from the return port of the seperator is laminar when it goes into my catcher bottle).
Effectively I seem to have a mixture that can never be set right it seems.
I'm going to be away for about a week without access to the car. I'll likely take the carb apart and rebuild it, replacing everything and measuring it all up properly i stead of my previous half-assed cleaning of it when I get back on the weekend, but I thought I would make this post to see if anyone might be able to point out a very obvious problem, or potentially point me in the right direction.
I tried to put as much detail in this post as possible, so if you read the whole thing, thanks very much for your time.
Timeline:
- Got the car on the road after sitting for a few years
- Ran happily for about a month
- Started developing intermittant hesitation when pulling away from stopped - every now and then the revs would dip from idle and take a second or two to build back up
- About two days later it did the above pretty much constantly. On my way home it suddenly started lurching and struggling regardless of what gear I put it in, and I had to struggle to get it off the road without stalling.
Fuel seemed to be getting up to the carb fine - there was the tiniest little air bubble in the top corner of the inline filter, and I had also replaced all the fuel lines and jubilee clips.
On the ignition side of it, I had before getting the car on the road replaced essentially the entire ignition system: spark plugs, ht leads, tci, dizzy rotor, coil.
This led me to believe that the problem lay somewhere with the carb, thinking it might be a gunked up jet or drilling or something similar, so I ordered some bits up and did the following:
- Split apart in order to spray out the jets and all the gunk inside (I collected loads of soot particles and some bigger solid chunks)
- Took the waxstat off and verified it extended with heat properly
- Replaced and readjusted the PDU (it was cheap enough I thought it a better option than getting a guage and what not to test it). Set to 2.5mm when sucking on the vac line, 4.9mm when pushing on the little bolt at the back.
- Cleaned all the shit out of the housing for the autochoke, and put it back on
- New red gaskets with rod + oring end cap thing that is shaped like a rounded parallelogram and sits on the side (can't remember what it is for)
- New gasket for the accelerator pump, made sure it was the same size as the old one
- New gasket between the two halfs of the carb
- New carb flange
- I took the inlet manifold off and the coolant channel grommet was positively shredded, so new grommet and gasket
- Replaced the vacuum lines of the carb with 4mm inner diameter lines.
- Replaced the o'rings on the 3 point and put some thin grease on them.
- Put a compression tester guage on all four cylinders and it had good compression
- 1kohm across each ht lead
- 1kohm across rotor cap
- 0.7ohm from top to bottom of the spark plugs
- Spark plugs are a bit black / wet from fuel
- Solenoids click when the electrics are on
- 12v to both solenoid plugs
- 0.7ohm from carb to battery -ve
- 14.9ohm between autochoke lead and battery -ve
- 12v to manifold hedgehodge
- I had no 12v to the autochoke, but there was 12 going into one side of the sender, and I did have the engine running about half an hour ago, with the choke flap opening it self, so I believe the coolant may be warm enough that it is turned off. I will check next time I am home.
- Waxstat extends properly and retracts with a small amount of pressure
After a lot of trial and error I found that screwing the mixture screw (the one accessible via the bung on the airbox) fully in, then unscrewing it by two full turns seemed to allow the engine to start without the carb popping and spewing a ton of smoke.
This is what happens when starting it up:
- Goes up to 1.1k and seems to sit there steadily
- Weirdly it doesn't do the 2k blip it used to do
- Can put my foot on the throttle and rev it up happily to 2k
- After a minute from starting I took the air filter out and glanced at the choke flap - it was wide open at this point (having started just about closed).
- I left it for 5 minutes and over that period of time it dropped to about 900 and seemed happy with that. I could still rev it up to 2k happily.
- Throughout all the above it was spewing a blanket of petrol smelling blue tinged smoke over the drive and it sounded really burbly
I subsequently came back after a few hours to let it sit and go back to "cold"/ambient temps for the purpose of repeatability and tried the same but turning the screw counter clockwise. Effectively the same thing happened.
I also ran the engine up once, messing with nothing, just letting it get hot, and it seemed happy to throttle up, but was stilling spewing smoke everywhere.
While running the fuel filter was chock full of fuel, and after it cut out there was still plenty of fuel in the filter. The mechanical fuel pump and air/vapour seperator/pressure regulator have both been replaced. It used to struggle to start and I had to pump the throttle once or twice depending on how long I had left it without starting it for the couple of months when I got it ready to go back on the road, after replacing the air/vapour seperator it would start happily when turning the key, now I have to give it a pump to get it run, but it may just be that method of bleeding the air doesn't get all the air out (I split the return line, blow air into return to the tank, let the fuel filter all fill up and make sure the flow from the return port of the seperator is laminar when it goes into my catcher bottle).
Effectively I seem to have a mixture that can never be set right it seems.
I'm going to be away for about a week without access to the car. I'll likely take the carb apart and rebuild it, replacing everything and measuring it all up properly i stead of my previous half-assed cleaning of it when I get back on the weekend, but I thought I would make this post to see if anyone might be able to point out a very obvious problem, or potentially point me in the right direction.
I tried to put as much detail in this post as possible, so if you read the whole thing, thanks very much for your time.